DRAFT: This module has unpublished changes.

Day 1 – 5/30/12

-          Set up computer area and computer

-          Read articles about microphones and directional determination

-          Got organized

 

Day 2 – 5/31/12

-          Finished chapters 3 – 6 from MATLAB book

-          Turned in direct deposit

-          Got info sheet filled out

-          Emailed Milutin

 

Day 3 – 6/1/12

-          Finished Chapters 7 – 8 in MATLAB book

-          Looked at many different Wiki pages on the ear and hearing

-          Worked to understand papers

 

Day 4 – 6/4/12

-          Finished chapters 9 – 11 in MATLAB book

-          Got as far as I could in my understanding of the microphone systems

-          Annotated my understanding

-          Printed MATLAB notes

 

Day 5 – 6/5/12

-          Wrote out and understood more of the algorithm

-          Found out my actual project (programming the bot)

-          Spent time researching the robot

-          Got instruction manuals for the Robot

 

Day 6 – 6/6/12

-          Figured out Taylor Series

-          Found more parts to the bot

-          Took the bot apart and put it back together

-          Set up another computer

-          Looked at the code for the program algorithm

-          Thought I broke the robot and the transistor trying to prop it open

 

Day 7 – 6/7/12

-          Tried multiple configurations for the robot

-          Got it to work in autonomous mode

-          Spent the day trying to figure out Serial Connections

-          Tried different computer

-          Tried switching the wires

-          Downloaded some Terminal Emulators programs for the computer

-          Printed out Instructions

 

Day 8 – 6/8/12

-          Printed out Research Papers

-          Tried to solder a 6th connection – failed

-          Connected bot to computer with the pins reversed

-          Turned on robot and it got connected

-          Worked for a little bit

-          Computer had exception issues, bot ceased to function

-          Worked on E-Portfolio

 

Day 9 – 6/11/12

-          Most frustrating day in the lab thus far

-          Couldn’t get bot to go in autonomous mode

-          Got bot to connect to computer once, wouldn’t connect anymore

-          Tried to redo connection wire, I think I did it wrong

-          Bot freaks out every time I try to plug it in

-          Tried Khepera I, didn’t work either

-          Going to try to get bot to work again tomorrow

 

Day 10 – 6/12/12

-          Got Khepera to work in autonomous mode

-          Got it to work and hooked it up to computer

-          Rebuilt the serial line wire

-          Figured out MATLAB configuration

-          Trying to open the serial port in MATLAB

 

Day 11 – 6/13/12

-          Couldn’t get Khepera to communicate with MATLAB

-          Tried many different serial ports

-          Tied compiling the code many different ways

-          Wrote on Khepera forums

 

Day 12 – 6/14/12

-          Checked forums, got answer

-          Couldn’t’ get MATLAB to work originally

-          Turned on old computer because COM1 wasn’t available

-          Found old files and projects and looked at history

-          Finally got Khepera to work in MATLAB

-          Transferred old files to new computer

-          Got Khepera to work with MATLAB on new computer

-          Neatened work area and computer

 

Day 13 – 6/15/12

-          Tried to write a simple code for Khepera in MATLAB

-          Robot was not functioning as expected to

-          Read papers on the sound chip and the project

-          Tried to figure out how to hook up the acoustic chip

 

Day 14 – 6/18/12

-          Tried to figure out why Khepera wasn’t working

-          Had maintenance guy look at broken resistor

-          Printed many documents on buses

-          Hooked up general turret to Khepera

-          Emailed Milutin about schematics

-          Read about circuits

 

Day 15 – 6/19/12

-          Continued to work with Khepera

-          Went through the LabVIEW tutorials

-          Learned the workings of LabVIEW

-          Read through Bus Connections and Turret Specifications

 

Day 16 – 6/20/12

-          Got Khepera to work with LabVIEW

-          Revised Grad Essay

-          Read through some more papers and tried to understand the algorithm

-          Looked at KTProject

-          Found files for KTProject

-          Emailed Milutin asking for the schematics for the chip

 

Day 17 – 6/21/12

-          Meeting with Milutin

-          Found other chip

-          Tested Acoustic Chip

-          Learned about Electronics equipment

-          Installed AC

 

Day 18 – 6/22/12

-          Learned how to download programs onto the bot

-          Tried to do autonomous mode

-          Posted to forums, tried to figure out autonomous

-          Mode 0 stopped working

-          Printed out KTProject tutorials

-          Learned about KTProject

 

Day 19 – 6/25/12

-          Got bot to work in mode 0

-          Got bot to download code and run in autonomous mode

-          Figured out how to attach serial cable and chips

-          Read the diagrams and tried to figure out how to interact with the chip

-          Read some old MATLAB files

-          Found new MATLAB commands

 

Day 20 – 6/26/12

-          Met with Milutin, discussed robot

-          Tried to figure out Robot with Chips

-          Figured out addressing

-          Looked up address and bus information

-          Looked at Bios Information

 

Day 21 – 6/27/12

-          Spend more time researching the buses and connections

-          Tried to figure out connection

-          Wrote MATLAB code for easy testing

 

Day 22 – 6/28/12

-          Spent all day going through the FPGA

-          Tested the digital chip

-          Tested the ICs on the chip

-          Researches buses and connections

-          Revised MATLAB code to make it more efficient

-          Emailed Milutin about the code

 

Day 23 – 6/29/12

-          Spent the day trying to figure out FPGA for the robot

-          Asked Shuo for help

-          Tried testing just the bottom chip

-          Still unable to program the bot

-          Not sure what the next steps are

 

Day 24 – 7/2/12

-          Hit a rode block in the project

-          Began to look over some of the documentation for the project

-          Read and reread papers to understand gradient flow localization

 

Day 25 – 7/3/12

-          Spent the whole day reading for increased comprhension of the material

 

Day 26 – 7/5/12

-          Looked at the connections

-          Tried multiple different connections

-          Tested the circuits multiple times

 

Day 27 – 7/6/12

-          Tested things through the computer

-          Tried to look up information online

-          Looked at FPGA some more

-          Tried to draw generalizations

-          Emailed Milutin about the code, what kind of input it is

 

Day 28 – 7/9/12

-          Developed the code for the robot

-          Thought about inputs and outputs

-          Looked at the old code

-          Figured out microphone layout

 

Day 29 - 7/10/12

-          Tried to figure out the code more

-          Made improvements

-          Tested with oscillator to see what isn’t working

-          Tried to run the programs with the oscillator

 

Day 30 – 7/11/12

-          Tested the chip with the oscillator again

-          Tested the chip with single wire connections

-          Identified the reset pin as the problem

-          Robot stopped working with the turret

-          Tested attaching the Vcc to Reset

 

Day 31 - 7/12/12

-          Tested the robot with multiple connections

-          Tried to program the robot with just the other cables connected

-          Not working

-          Tried to troubleshoot some more

-          Couldn’t get anything done

 

Day 32 – 7/16/12

-          Couldn’t get anything done

-          Couldn’t meet with PI

 

Day 33 – 7/17/12

-          Talked with Milutin

-          Planned to test the chip by itself

-          Obtained necessary materials

-          Attached chip to breadboard with various wires

-          Drew diagrams with color schemes

 

Day 34 – 7/1812

-          Tested the chip on the breadboard

-          Getting back a short circuit

-          Hooked up power supply directly to chip to determine issues

-          Need to re-wire

-          Found switches to use

 

Day 35 – 7/19/12

-          Tested the breadboard configuration

-          The current was jumping up and down

-          Figured out we didn’t need 4 of the pins

-          Took the rig to Tony’s, couldn’t get it to work with a clock signal

-          Rewired the bread board so it is easier to test

 

Day 36 – 7/20/12

-          Tried to contact the Scott, wasn’t available

-          Wrote him an email

-          Worked on my research paper

-          Took pictures for my posters

 

Days 37 - 44 - 7/23/12 - 8/1/12

-          I focused the majority of my time developing my abstract, poster, and research paper

DRAFT: This module has unpublished changes.